With 120 miles to go, we realized that we could no longer make any plans that included hoping for the wind - there was none. We knew that we were low on fuel so we started doing some calculations to see just what our situations was, and the result was that making landfall on the diesel that we had was questionable at best.
So, the last resort option came out and after a few hours of discussion, we decided to pull the trigger. We stopped the boat, lowered the dinghy and moved it around to the starboard side of the boat and rigged a spring line from Stray Cat's aft cleat to a padeye on the front of the dinghy. We then rigged the dink's bowline to Stray Cat's bow cleat. When all was tight and looked right, we revved up the Yamaha 15hp, and off we went - at a blistering 2.5 knots. The dink was doing an admirable job pushing us along, and for as long as we could keep that Yamaha running, we could move along at 2 to 3 knots without running the diesels, thereby conserving fuel that we would need to make landfall and enter the harbor. We also had a nice current of 1 knot and managed to stay between 3 & 4 knots most of the time. We were carrying approximately 14 gallons of gasoline on board, but none of us were sure of how long that amount would last because none of us had much experience pushing a 22,000 pound boat with a 15 hp outboard motor.
We started with the "Dinghy Push Project" at about 9am on Sunday morning. At about 11am, a squall came up and we were able to get the genny out and pulling for about 2 hours, which helped the dink get us up to 5 or 6 knots. Finally, at around 5pm, the first 4 gallon fuel tank ran dry, and we switched to our second 4 gallon tank. Then right before dark at about 7pm, we switched to the larger 6 gallon tank so that we would have the least possible chance of having to make any adjustments to the dinghy during the night, when it would be infinitely more dangerous.
We "motored" through the dark for hours, and then at 5am, on Capt. Mark's watch, the Yamaha finally sputtered and died. Back to slow motoring on one diesel engine until sun-up, but by that time, we had come within 30 miles of Panama, and because of the heroic actions of our little 10 ft dinghy and 15hp Yamaha, we were now pretty confident that we had enough fuel to make landfall and get into port. The dink had pushed us for almost 24 hours and helped us make almost 60 miles. Not quite as good as having the trade winds on the beam, but it got the job done. The next morning we tried to get the dinghy going again, but the motor wouldn't start - it seems that during the night, the strengthening waves had splashed into the dinghy and some water had entered the fuel tank. Capt Mark proceeded to take apart the carburetor and clean it at least twice - all while underway, but alas, it didn't help as the gasoline was now contaminated.
Oh well, at least we made it to Panama.
Tuesday, October 30, 2007
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